Monday, June 14, 2010
Bluebirds are GO!
I'm by no means complaining, it just means that there was no eventful stories or anacdotes to blog about. So I skipped it! All I really had to do with getting the engine in was to make sure everything was in the right place, reconnect some earths and turn the key. We did have some dramas at first when it finally came to starting the engine. See it would kick over but not start. So we did the usual fault finding things (yay, fault finding....), check for spark, check for fuel, and there was our problem. No fuel. Turns out we pulled the fuse for the fuel pump when we first started so it wouldn't spray fuel every where when we turned the car on. With the fuse back in place we tried again. No luck! The battery we were using had carked it, so we put the jump starter on charge and messaged Red to see if he could help. An hour later Red came over with his battery, connected it up and it had life. Idled like shit, but alive nonetheless.
So everything (apart from the idle) seemed good. Once it warmed up it idled well, Glenn brought his 400 year old timing light over and fixed the timing, and all seemed to be going well...until we looked under the car. There was a massive leak. Possibly rear main seal. Too big to let go.
So now the engine has to come out again. *Sigh* But in saying that with the engine out the clutch engagement point (the floor) can be changed to a more reasonable spot and also clean out/replace the IAC valve (which should help the cold idle...hopefully), which is in a bitch of a spot to get to. There was two IACV's that we could choose from, one from the original engine and one from the one I bought, no idea which one we used and not 100% sure if changing it will help, but there is only one way to find out.
So, long story short, its back to where we were 6 months or so ago.....shit balls! At least I dont have to do anymore sanding, eh, painful!
Sunday, May 2, 2010
Putting the pieces of the puzzle back together!
So with the body work all done (minus putting the front bumper and head lights on), it was time to move on to the next part - reassembling the engine. With the bits and pieces I had lying around this was going to be interesting.
So we worked out what was needed and I set about trying to find parts. Mostly I didn't need to much, and the parts I needed weren't too hard to find (thankfully). So on one of my days off myself and Gren set out to pick up gaskets, oil seals for my distributor and a clutch. Autobarn was the first stop, then Nissan spare parts at Petrie (which didn't have my parts yet) then to Albion. At the recommendation of Glenn and Red I got my clutch from Direct Clutch Services (and after the help and assistance I got from Jerry, I would suggest them to anyone!). So after the 20 min wait for the clutch and the journey to the atm that only had $20 notes ($600 in 20's is extremely awkward!) we headed home.
The following days were then followed by piecing the engine back together...well not the engine, but the bits connected i.e. the inlet manifold brackets etc. Which didn't take quite as long as originally thought, so it was onto the gearbox side. Time to fix the original problem, the throw out bearing! With new bearing on and (hopefully) working smoothly, we re-assembled the flywheel and clutch assembly and then wriggled the gear box and transfer case onto the engine....makes it sound so easy.
Thursday, March 25, 2010
Painting - The Home Stretch!
Looks a lot better. If you can recall back to what it originally looked like...
Then came the panels...
Front and rear bumper's turned out brilliantly!
Then came the body...
This is the closet we came to assembling it. The final clear coats make the blue really shine! Looks pretty good...if I do say so myself.
The only thing left to do now is assemble it...hope we don't scratch anything! (Oh and another sanding. I hate sanding).
**Note: I'm now up to date with my blog, obviously I haven't done all of this work in a few weeks. Its taken months, but there was no point only telling half the story. So this is where I currently am in the project. Any updates from now will be on an as-they-happen basis!! I can't wait!
Painting - Colour Change!
So here is the first ever bluebird blue bits! It was exactly how I thought it would look!
Sunday, March 21, 2010
Painting - Preperation!
One of the most serious bits in need of repair. Not that mine and Red's "fix it with a rubber mallet job" wasn't any good.... or so we thought at the time.
Sunday, March 14, 2010
The Engine
- HKS cams
- HKS solid valve springs
- Port and polished head
- Full rebuild including forged pistons and rods
- Cometic head gasket
- ARP head studs
- Rocker kit
Saturday, March 13, 2010
The Other Option
Homeward-bound: one of our last coffee/dinner stops before home. We were somewhere outside Newscastle.
Everything went realatively well, except for the fact that we didn't exactly know where we were going. (As many of you may know, E-Bay gives a suburb, but not an address when you look at an item). Good thing I had an iPhone (with the ebay app! lol) As the engine ended late Friday night and we left early Saturday the seller didn't have a chance to contact us, so we were technically driving blind. Long story short, got in contact with the seller, got to his workshop, picked up the engine, came home. 5:15am Sunday morning. Over 24 hours of straight driving....good thing we took a large car. But the effort was worth it.
SR20, in its new home. The barn floor...
Edit (Jen): For me it was an agonizing journey filled with "Brendan! Are you awake! Hello? What's your favourite... colour? food?' Trying to keep our drivers awake and away from kangaroos. It was scary at times, such as the drive into Ballina when Brian was driving and I was chatting to him from the back seat, while Brendan slept in the front. We'd come accross some dense fog and the only indication of what was ahead were the tail lights of the trucks in front of us, it was safest to stay behind them because we couldn't see a thing on our own. This was around 12:30am, when tiredness was also becoming a critical factor.
Looking back, it was a pretty big gamble - trying to achieve 2000km in 24 hours, 2 drivers and only food stops. But we got there, and we got home... and then we slept for quite awhile!
PROPS TO JEN FOR NOT SLEEPING AT ALL THE ENTIRE TRIP!